Editor's Choice


Control loop: Case History 179 - Some unusual measurement and control problems

September 2021 Editor's Choice

As I have often mentioned, many people do not know how to set up control on PLC/scada systems properly and errors in control and measurement often result.

Admittedly I have found similar problems in DCS control systems, but much more rarely. I think this is because DCS systems are usually found in plants where there is a strong control ethos and people in the manufacturing teams have a better understanding of control and measurement. Also, DCS systems have many more safeguards built into them to prevent users making mistakes than do most PLC/scada systems.

Problems with a nitrogen flow control loop

The example given in this article illustrates some mistakes made by the system integrators and control engineers at a metals extraction plant that used a well-known make of PLC and scada for its controls. The C&I; staff in the plant had not picked the errors up and had been working for years with the problems. The loop in question was an important nitrogen flow control feeding an hydrogen sulphide reactor.

Whenever one optimises a control loop, it is essential that you first discuss the control in its entirety with the people who look after the control side of things, as well as with the people who really understand the process. In many plants they are the same people, but often I find that people on the control side do not really understand the process and vice versa, people on the process side often don’t understand controls.

Typically, we investigate and discuss the following:

1. Details of the process.

2. The configuration of the control loop.

3. The control strategy.

4. The purpose of the control.

5. How quickly the control must react. For example, sometimes they want it as fast as possible, or maybe it must be kept slow so as not to disturb things downstream. Sometimes it doesn’t really matter and it is fine if it operates mostly in the right region.

6. What external factors can affect the control and can this loop affect other controls or processes?

7. Details of the measuring system.

8. Type of valve.

9. Problems that are being encountered with this control.

In the case we are discussing here, the two main problems encountered by the operators and process engineers were firstly that the readings didn’t tie up with laboratory measurements and mass flow balances and secondly, the control was not satisfactory, being slow and hardly ever getting to SP (setpoint).

On investigating, it was discovered that the range set in the PLC was incorrect. The actual flow transmitter range was set to 0-1125 m3/h, but the figure that had been programmed into the controller’s PV (process variable input) was 0-1200 m3/h. On top of this, the transmitter signal coming into the PLC was first divided by 1,25, as the process people wanted to see a mass flow range of 0 -900 Nm3/h and not volume flow figures. This explained the discrepancy observed by the process people.

The next problem observed was that the flow signal was running at about 5% of the full-scale reading. This is potentially very bad. As a rule, very few flow measurements are accurate and reliable so low down in the range and may even be incorrect, which does depend on the type of measurement and the transmitter’s rangeability. Unfortunately, at the time of the testing, no one was available who could advise on the details and specification of the transmitter.

Optimising the loop

The first live test carried out on the loop is nearly always a closed loop test with ‘as found’ tuning, where setpoint changes are made on the loop with the original tuning (in this case P = 0,5 and I = 10 sec/repeat). There was also a lag filter with a time constant of 2,45 seconds inserted in the PLC before the PV input to the controller. The test is shown in Figure 1 and the following observations were made:

• The transmitter is working far too low down as discussed earlier.

• The tuning is incredibly slow and takes far too long to follow setpoint.

• Although the filter is relatively small there is no need for it, as filters introduce other problems. (Discussed in other articles).

The open loop test (in manual) is shown in Figure 2. The filter has been removed. It can be seen that:

• The process gain (the ratio of the steps in PV to PD, the controller output) is about 0,3, which would indicate the transmitter is probably over-spanned by a factor of three.

• There is very slight non-linearity in the installed characteristics, which is not serious.

• The valve has an overshoot when moving in the closing direction. This is not particularly serious but could cause a stick-slip cycle when the loop is in automatic with better tuning. Possibly it could be eliminated by tuning the positioner a little better.

• Apart from this the valve is working very well.

The controller was then tuned using the largest step in PV (for safety). The Protuner gave a medium tune of P = 0,4, and I = 1 sec/repeat.

The final closed loop test with the new tuning is shown in Figure 3. It can be seen how well the control now works and it is about 15 times faster than the original tuning. This is an example of what we often find when performing loop optimisation where lack of knowledge of the practicalities of control results in underperformance and in this case, imparting incorrect information.


About Michael Brown


Michael Brown.

Michael Brown is a specialist in control loop optimisation with many years of experience in process control instrumentation. His main activities are consulting and teaching practical control loop analysis and optimisation. He gives training courses which can be held in clients’ plants, where students can have the added benefit of practising on live loops. His work takes him to plants all over South Africa and also to other countries. He can be contacted at Michael Brown Control Engineering, +27 82 440 7790, [email protected], www.controlloop.co.za


Credit(s)



Share this article:
Share via emailShare via LinkedInPrint this page

Further reading:

Machine health monitoring with ifm
ifm - South Africa Editor's Choice IT in Manufacturing
With ifm’s machine health monitoring, early signs of wear can be detected and unexpected failures prevented. Combined with equipment preventive maintenance software, interventions can be scheduled proactively to avoid costly downtime.

Read more...
Powering Africa’s sustainable mining
VEGA Controls SA Editor's Choice Level Measurement & Control
At the 2026 Mining Indaba in Cape Town, one theme rises above all others, progress through precision. For VEGA, a global leader in process instrumentation, this mission aligns perfectly with its core purpose, which is turning measurement into meaningful progress.

Read more...
PCS Global delivers turnkey MCC installation in Botswana
PCS Global Editor's Choice PLCs, DCSs & Controllers
PCS Global is delivering a turnkey containerised MCC installation for a major copper mining operation in Northwest Botswana.

Read more...
SEW-EURODRIVE transforms drivetrain uptime
SEW-EURODRIVE Editor's Choice Motion Control & Drives
The DriveRadar IoT Suite from SEW-Eurodrive is an ideal solution for industrial condition monitoring. This powerful ecosystem of intelligent sensors, edge devices and cloud-based analytics ensures that customers have full visibility and control of their operations.

Read more...
Loop Signature 31: Non-linearity in control loops (Part 2)
Michael Brown Control Engineering Fieldbus & Industrial Networking
This article is a continuation of Loop Signature 30 published in the last issue in this series, exploring reasons for non-linearities which may be encountered in feedback control loops

Read more...
PC-based control for flat wire motors for electric vehicles
Beckhoff Automation Editor's Choice Motion Control & Drives
Special machine manufacturer, ruhlamat Huarui Automation Technologies has unveiled the second generation of its mass production line for flexible stators with bar winding (pins). This enables an extremely short production cycle and line changeover times, supported by PC- and EtherCAT-based control technology from Beckhoff.

Read more...
Heavy impact, smart control
Axiom Hydraulics Editor's Choice Pneumatics & Hydraulics
Every now and then a project lands on your desk that’s equal parts heavy machinery and fine control - a tantalising mix for any engineer. A client approached Axiom Hydraulics with a project exactly like this.

Read more...
Pneumatics makes a technological leap with the proportional valve terminal
Festo South Africa Editor's Choice Motion Control & Drives
Festo continually makes bold technological leaps to keep pace with global advancements. Controlled Pneumatics is redefining the boundaries of compressed air technology to meet the demands of today’s most advanced applications.

Read more...
Driving fluid power forward
Editor's Choice News
The National Fluid Power Association is developing its latest Industrial Technology Roadmap for 2025, showing how hydraulics and pneumatics are changing to meet new industrial demands.

Read more...
World’s hottest engine
Editor's Choice Motion Control & Drives
Scientists have built the world’s smallest engine. It’s also the world’s hottest. It could provide an unparalleled understanding of the laws of thermodynamics on a small scale, and provide the foundation for a new, efficient way to compute how proteins fold.

Read more...









While every effort has been made to ensure the accuracy of the information contained herein, the publisher and its agents cannot be held responsible for any errors contained, or any loss incurred as a result. Articles published do not necessarily reflect the views of the publishers. The editor reserves the right to alter or cut copy. Articles submitted are deemed to have been cleared for publication. Advertisements and company contact details are published as provided by the advertiser. Technews Publishing (Pty) Ltd cannot be held responsible for the accuracy or veracity of supplied material.




© Technews Publishing (Pty) Ltd | All Rights Reserved